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![]() ![]() Research showed that the loco named 'Temeraire' was built in 1989 (so it was much younger than I imagined) and that Mardyke are still trading today, which was useful as I could purchase some parts as "off the shelf" spares. The photo on the left taken after the loco had been rebuilt shows the parts from my "for possible use bucket". All these parts, and a lot more that were too bad to even be considered for reuse, ended up in the scrap bin. Without the Internet it would probably have been impossible to rebuild the Hymek and even so it often took hours of searching to find a supplier for some of the rarer BSF and BSW nuts and bolts. As usual the restoration went well over budget; however the end result is not only a useful loco but the preservation of an engine produced by Mardyke that may otherwise have disappeared. During my research into the history of this Hymek I learnt of other Mardyke Hymeks that were being scrapped as "beyond economic repair" so preserving this one to me at least has been worthwhile. The following sections of this page show some of the major components of the Hymek in "before and after" photos to give an idea of the work involved in the restoration. But if you only want to see some photos of the finished Hymek, now renamed 'Dark Star' then please click here. |
The Power Bogie |
![]() As the power bogie was dismantled it became apparent that both of the aluminium drive pulleys on the engine had worn so far that the new drive belts I had purchased were running on the flat bottom of the pulley as opposed to gripping in the "V". New pulleys weren't too hard to find, but they had to be bored, faced, and reamed to fit; and keyways had to be cut. I also discovered that the mounting bracket for the Hydrostatic drive was welded in such a way that the pump was not aligned to the bogies axis with the result that both the belt and chain drives operated through angles. As the bracket could not easily be removed and rewelded I opted for tapered wedges to align the Hydrostatic drive. Thankfully the drive pulley on the engine could be got into correct alignment by facing its boss to the correct length. Mardyke were able to supply new wheel sets fitted with axles and drive sprockets from stock as well as the axle bearings, and consumable spares (spark plug, air filter etc.) for the Briggs & Stratton engine came from the local mower shop. The correct silencer for the engine was also quite easy to obtain, but I had to have the exhaust pipe bent to my own drawing from 1" diameter by 16 swg steel pipe by Merlin Motorsport. For some reason the new sprocket for the Hydrostatic unit supplied by Mardyke would not fit so a suitable sprocket and chain were obtained from Parkside Electronics. Both the engine and Hydrostatic drive were flushed through several times with fresh oil until it ran clear when drained to remove the "black stuff" that may once have been oil. All the metal components of the bogie were grit blasted, primed, and repainted before reassembly and you can see the completed power bogie in the photos below. My thanks go to Simon from All Welding Work in Kingsley Hampshire for the nice job he did on these bogie parts. ![]() ![]() |
The Unpowered Bogie |
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The Control Panel |
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The control panel is constructed from Birch plywood, laser cut and laser engraved; the lettering being filled with black (using a 6B pencil) before the panel was varnished. It's the first time that I have tried this technique which, although much cheaper than having a metal panel cut and engraved, results in (at least to my eyes) an acceptable panel as opposed to a "perfect" panel. |
The Body |
The
body was always going to be something that I had to subcontract for
grit blasting and paint spraying as it was simply too large (at over 8
feet or 2.4 meters long) for me to spray with aerosol paints in my back
garden. Naively I had imagined that blasting and painting
would
be the only work required, but I had missed the fact that the loco must
have been involved in an accident sometime in its past which had
resulted in a pronounced bend in the body panels on the left-hand side.
Sorting that out gave me the chance to practice panel
beating,
but I didn't expect to have to use a 4lb club hammer ! The
Mardyke body was certainly very rigid, which meant that the accident
must have involved some major collision or even a roll over.
Eventually I got the body straight and various loose parts
and
unwanted holes welded, with sanding discs on my angle grinder
creating nice smooth body contours. It was all
rather
reminiscent of those days I spent in the 80s building and maintaining
my Land Rovers. Many months later than expected I sent the
body
to my local "finishers" for grit blasting and painting. I can
really recommend Goldburn Finishers in Bordon, Hampshire, as they did a
superb job of spraying the various colours needed to create the classic
Hymek two tone green colour scheme. I think it turned into a
"labour of love" for them, and I know that they did their own research
into the full size Hymeks as well as following my detailed painting
instructions. Apparently having such a large loco on display
in
their workshop while they worked on it provided a great deal of
interest for their customers. When we dismantled the Hymek at Pinewood it took six of us to lift the body off of the bogies. When it came to reassembly I had to work out how to fit the body over the assembled power bogie by myself. Thankfully I still had the electric winch that had previously been fitted to my van to pull the 4" scale Tasker Traction onboard, and with a 2000lb pull rating it obviously would be able to lift the Hymek body. The photos below show the body being refitted, and literally the project was hanging by a thread during the process ! ![]() |
![]() Perched on the freezer (which serves as one of my work benches) you can see the Hymeks new 12v battery being used to operate the electric winch which has been bolted to one of the garage roof beams. |
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Horns & Vacuum Brake System |
![]() On either side at the top are the High and Low tone horns with their respective power relays, and hanging dead centre is the PNP vacuum brake servo which operates the brakes on the front bogie (the rear bogie brakes have their own handbrake in the drivers compartment). The two orange spheres are reservoirs for the vacuum braking system; the one on the right serving the vacuum brake servo and the one on the left being connected directly to the electric vacuum pump. Having a reservoir connected directly to the pump gives the pump a significant volume to evacuate which stops the vacuum limit switch chattering (a problem I have seen on many electric vacuum pump systems). The two reservoirs are actually 6" diameter ballcock floats fitted with homemade pipe connectors, and you can buy both and still have money left over compared to the cost of the traditional commercially available vacuum reservoir. The rather over exposed (shiny) thing halfway up the left hand support is the vacuum limit switch that controls the electric vacuum pump which can be seen behind the support frame. The 12 Volt battery will eventually be fitted in the framed area in the foreground, and the main and individual circuit fuses are fitted respectively to the right and left of the battery tray. Totally hidden by all of this are the LED locomotive running lights and their junction boxes. Wiring and plumbing this assembly took over 11 hours mainly because of the space limitations and the need to ensure that the assembly had suitable wiring and plumbing connectors to permit it's removal if / when service is required. Fitting the entire plumbing and wiring system for the Hymek has taken almost a week which seems like a long time, but in reality there is more to fit and wire than on some of the Land Rovers I used to build and race in the 1980's and they had considerably more space to fit everything in to. |
Finished (at last !) |
![]() Thankfully once the wiring was completed every feature worked when tested. All that remained was to fit the loco numbers and nameplates. Finally on the 367th day after I had started work the Hymek was completed and three days later, having managed to squeeze it into my VW Caddy MPV, the Hymek was tested at Pinewood. The loco worked perfectly pulling empty coaches around the track, but subsequently proved to suffer from a lack of tractive effort when it started to hail passenger trains. Initially it wasn't clear if the problem was caused by the EATON hydraulic unit or by some other factor, but testing soon showed that it was simply a case of the drive wheels slipping on the track. Despite its size and weight the Hymek is rather a poor performer when it comes to hauling passengers around Pinewood as even on dry track it is quite difficult to find enough traction to drag two loaded coaches out of the station despite having 6.5 horse power available from the engine. As designed by Mardyke the four driven wheels on the power bogie have no suspension to keep them all in contact with the rails, and even with the best laid track I would guess that only one wheel on each axle is really carrying the weight of the engine. The end result is effectively a two wheel drive locomotive and that is never going to be a load puller. |
![]() Sadly after operating passenger services at Pinewood on just three occasions I left the society, and due to the lack of use and difficulty of transporting such a large locomotive I decided to sell it. As is so often the case the Hymek sold for much less than it cost me to buy and restore it, but I know that its new owners will be making good use of it. If you want to follow the Hymek's progress then take a look at the Fancott railways website at www.fancottrailway.co.uk or their Facebook page at www.facebook.com/FancottMiniatureRailway |
Photo Gallery |
The
photos below were all taken by Pinewood member Paul Konig during the
Hymek's trial run at Pinewood on July 6th 2014. To watch a short video of the Hymek running at Pinewood click here.![]() |
![]() 'Dark Star' ready to depart from Pinewood Central station. The wagon directly behind the engine is there to stop young passengers from trying to remove the rear windscreen wipers. |
![]() In this photo you can see how the Mardyke design has tilted the loco body (the wagon is riding "flat" on the track) into the turn to aid stability. |
![]() The lighting on 'Dark Star' is now all done using LEDs. |
![]() In this photo you can see that the windows give a nice reflection without letting you see through (or looking like mirrors). The windows have been made from mirror finish polycarbonate with the surface lightly rubbed with fine wire wool. |
![]() Pinewood's two passenger hauling petrol / hydraulic locos together in the station. |